Saturday, October 4, 2014

AC/Blower Motor

A couple weeks ago I recharged the AC to see if that is all it needed to work. Sure enough once I got enough freon in there the compressor clutch kicked in and it was blowing cold. Everything was working fine until the other day the fan wouldn't come on. The clutch on the compressor was still engaging so I knew it was something with either the fan or electrical. The fuse hadn't blown so I checked the resistor on the back of the ac duct. Everything seemed fine there as well. I lowered the fan/dash

and found pieces of a rubber gasket from behind the dash had fallen in the fan, and it was stuck in place. Pulled the pieces out along with some more rotted gasket back there and it fired right up.

Drum brakes and more

I had a bachelor weekend this weekend so I decided to get some things done that were going to take some time. First thing I did was reseal my valve covers. I have had some smoking under the hood and I'm trying to find it by process of elimination. First up was the valve covers. I took them off, pounded the bolt holes flat so everything would sit flat and I used the Right Stuff gasket maker to seal them.

After that it was time for back brakes. I didn't know what I was getting into, but they actually weren't that bad. I ended up replacing the shoes, all the spring hardware and the wheel cylinders. The drums were in really good shape. The shoes actually were too, but I figured why not change them out while I was in there.






Pulling Parts

I found a junker about an hour and a half from here that had some parts I needed so I went out and pulled some stuff. I got the bumper (which had the original marchal fog lights), roof rack, and headliner board. I will update with more pics later, but the headliner board was in such good condition that I pulled it. I took off the old material, sanded it down and put new material on. I'm pretty happy with it.

Front Brakes

I haven't posted in a while, but I've still been working on the Jeep. About a month or so ago I took on the front brake pads and rotors. It was a little more involved than I thought. To get the rotor off you have to take the entire hub off which meant taking all the bearings out. While I was in there I repacked the bearings. Below are pics. The old pads and rotors were in very bad shape as you can see.
Old Rotor and bearings

All the pieces after unassembly


Old rotors, pads and grease seal

The old pads had worn deep ruts into the rotors

New rotor and pads

Tuesday, September 9, 2014

Dome Light Troubles

Alright, well I thought I had found the issue that was causing the failure of my dome lights. Just like most wagoneers the connections at pillar b were corroded. I was happy this was all it was...then it wasn't all it was. I realized after cutting the wires that they weren't hot either. I traced them all the way back to the front of the car to this connection, which wasn't connected. The previous owner has obviously done some major rewiring, but now I don't know what the wires are supposed to be running to? Any ideas?

Also, as you can see in the pic below the under the dash light is also disconnected. It would make sense to me that they would plug into each other, but the dome light connector is female 3 prong and the under dash light is male 2 prong. 


Sunday, July 20, 2014

Coolant Temp Sending Unit

While taking the intake off previously I broke the top of the old temp sending unit. I have ordered 2 of them now and they seem to be too big. I'm thinking the manifold expanded just a hair and made the hold slightly smaller than it originally was. The stinger of the new temp sending unit won't completely fit in the hole. It stops before getting to the threads. You can see what I mean in the pic below. That is pushed in as far as it will possibly go. This is the exact OEM replacement part mentioned on teamgrandwagoneer.com


New Lifters and Pushrods

Got the intake off, and the old valley pan was a MESS. Actually everything was a mess. This was a before pic.

After I got the valley pan out low and behold, the top of the broken lifter was just sitting there in the bottom of the valley. It really didn't look damaged, just not in the lifter where it was supposed to be. Below left is top of the lifter (the part sitting in the valley) and bottom right is the bottom of that lifter. Still in pretty good condition.

So, I pulled all the rocker arms, pushrods and lifters and replaced the old pushrods and lifters. Some pushrods were good, some were completely clogged. You can see through one here and not through the other.





While I had the intake off I took the opportunity to completely clean the valley and the intake. I also painted the intake and the valve covers to clean them up a bit. The last pic is the valley completely cleaned with the new lifters and pushrods installed.



After doing all this I put it all back together with the help of a friend, cranked her and she ran like a champ. 

Friday, July 4, 2014

Taking off the intake manifold

Alright, I've got most everything off the manifold now so that it can come out, but it's not wanting to budge. What am I missing?




Tuesday, June 24, 2014

Good vs. Bad Lifter

After having trouble with installing the new pushrod I decided that there must be something wrong with the lifter. After researching and getting advice from the forum my plan is to take the intake manifold off and see what is going on, and probably replace/rebuild the lifter. Before I start tearing into it I want to make sure what is going on with the lifter. So I bought a cheap usb snake camera to stick down the pushrod hold. Here is what I found. Pictures aren't perfect, but I think they show something. On the top is the bad lifter (as far as I know) and on the bottom is the good one (as far as I know).

It almost looks as if the internal part of the lifter is either gone or stuck in the down position. 

Saturday, June 21, 2014

Discovering new problems

Well, after buying new pushrods and rocker arm I went to install them this morning. I was planning on switching out both the pushrods. The problem is, on the exhaust side (where the broken rocker and sheared pushrod were) I can't seem to find the lifter for the pushrod to rest in. The intake side sits nicely in the lifter and even with all the other pushrods, but the other side doesn't seem to rest in anything until it is way too far down. It's as if there is no lifter there. I could actually wiggle it around enough for it to fall all the way down into it if I wanted to. Below is a pic showing where the exhaust pushrod wants to sit (WAY below where it's supposed to).

Friday, June 20, 2014

Broken Rocker Arm / Push Rod

After finding out that the popping was coming from the 8th plug I decided to pull the valve cover. I discovered that the pushrod had actually broken the rocker arm and come through it. It sheared the tip of the pushrod off and wasn't functioning properly. I have the parts coming in today so hopefully that will be the solution to the popping issue. I'm going to go ahead and replace both rocker arms and pushrods.


Tuesday, June 17, 2014

AC Compressor

After looking into the A/C system more we learned that these originally took R12 freon. I need to recharge my system, but I'm not sure if mine has been converted to R134-A or not. Can anyone tell from this photo?

Update: This had been converted. And I filled it up with R134 and it blew cold!

Help from Dad

My parents were in town this weekend so my dad and I were able to knock out a lot of little, but pretty significant stuff with the interior of the car. First, we installed a new track in the driver window. The previous owner had bought the track, but just left it in the back, so that was a free fix. Its working beautifully now.




The back passenger door wasn't opening so we managed to get it open and lubricate it really well. It's now opening and closing great. Also greased the window track while we were in there. While I was working on windows I decided to open up the tailgate and lube up that window. It was already working, but some new grease and a little cleaning and it is working great...very smooth.


While I was working on windows and doors dad was taking apart the dash. There was something electrical that was draining the battery when the car wasn't running. It turned out it was the radio. The previous owners had it for 3 weeks before they sold it, and the one thing they did was install a really cheap radio. Well it wasn't working correctly and was running 12 volts all the time. He got that fixed, and then we looked at the heater and ac. They hadn't been running, but after some testing of the blowers we found that everything is running. The A/C still isn't getting cold, but I'm hoping it just needs to be recharged. We also changed out some turn signal bulbs that were causing all the turn signals and hazards to stop working. And lastly we switched out the radiator hose because the old one was leaking. So, overall we got a lot of the little nagging stuff out of the way in a short amount of time, and for a grand total of $20.

Tuesday, June 10, 2014

Learning what everything is

Hard Steel line running from back of carb and it was just hanging loose. I ended up removing it and plugging the port on the carb.

Friday, June 6, 2014

Loud pop! Backfiring from the carb

So this is the popping that is coming from the carb. We think the culprit might be something under the valve covers. Hopefully nothing major broken.

Saturday, May 31, 2014

Lots of vaccum questions

There are a lot of hoses (I think vacuum hoses) that are missing or not plugged in. I need to find out where everything goes. This could definitely have something to do with the idling/stalling problems.



New Fuel Filter


This morning I switched out the old fuel filter for a new one. The old one didn't even have the bypass line connected. I also changed out the thermostat.